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6 Peter Nerenst Experience Share

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Service experience.

Greece Owners 2016-12-07


2016

MAN Diesel & Turbo


„Engineering the Future – since 1758.“

MAN DIESEL & TURBO .

Peter Nerenst. Operation MDT-CPH

MAN Diesel & Turbo PXN LEO  < 1 >


Cold Corrosion
Measures

Jacket Cooling Rating Dependent Load Dependent Cylinder


Bypass Basic Cylinder Liner Liner Cooling Water System

Alpha Lubricator High BN Oil


Mk. II Cylinder Oils distribution

MAN Diesel & Turbo PXN LEO  < 2 >


Cold Corrosion
Service experience

Design Implementation Product Maturing Service Experience

Load Dependent Cylinder Liner Cooling

Design Implementation Product Maturing Service Experience

Jacket Cooling Bypass Basic

Design Implementation Conclusion:


Product Maturing Service Experience

Rating Dependent Cylinder Liner


Cold Corrosion is Solved
Design Implementation Product Maturing Service Experience

Alpha Lubricator Mk. II

Design Implementation Product Maturing Service Experience

Oil distribution

Design Implementation Product Maturing Service Experience

High BN Cylinder Oils

MAN Diesel & Turbo PXN LEO  < 3 >


Piston Ring Development
Three decades of piston ring design

1st ring CPR

2nd ring CPR

3rd ring Gas-tight

4th ring

4 oblique-cut rings 4 CRP rings 3 CRP/gas-tight rings


Pmax 120 bar Pmax 140 bar Pmax 185 bar

Timeline

MAN Diesel & Turbo PXN LEO  < 4 >


Piston Ring Development
Introduction of 3-ring packs

S70ME-C8.2 G70ME-C9.2

MAN Diesel & Turbo PXN LEO  < 5 >


Piston Ring Development
Service experience
G70ME-C9.2 – 11,567 hours

G70ME-C9.2 – 12,302 hours

MAN Diesel & Turbo PXN LEO  < 6 >


G95ME-C9.5 Scuffing Incident

0-500Hrs  500-1000Hrs  Active scuffing

MAN Diesel & Turbo PXN LEO  < 7 >


Resulting contact marks

Old PC-ring New PC-ring

Polished area at first “bulb”.

MAN Diesel & Turbo PXN LEO  < 8 >


Liner deformation

MAN Diesel & Turbo PXN LEO  < 9 >


DCM (Deformation Compensated machining)

DCM made for lines already


manufactured or retrofit

MAN Diesel & Turbo PXN LEO  < 10 >


Cooling Jacket
New Design Original design

210mm

MAN Diesel & Turbo PXN LEO  < 11 >


PC-Ring
New PC-ring introduced for improved scraping effect
Original New

MAN Diesel & Turbo PXN LEO  < 12 >


11G95ME-C9.5, scuffing
First 3 x 8G95ME-C9.5  Later 11G95ME-C9.5 were delivered with
high second and third ring.

 Plan for latest action on above ring Constellation:


 Initial G95ME-C 9.5.  Additional CL grooves in top and second ring.
 Nice cylinder condition with above  Now Top 4 CLG, Second 2 CLG ,Lower 0 CLG.
piston ring con figuration.  Shift to earlier piston ring configuration,ie two lower rings.

MAN Diesel & Turbo PXN LEO  2016-09-23 < 13 >
Countermeasure

 Decreased inner diameter of the PC ring


 Introduction of full cermet coated piston ring packages
 LCD updating (also in function during load-up program)
 DCM (Dimension compensated machining) as to eliminate the
”thermal bulge”
 Introduction of 1 high 2 low piston rings (same as 8G95ME9.5
(Technomar)
 Introduction of long cooling jacket as to eliminate the bulge.
 Higher PC-ring
 Shorter cylinder liner (air flow vs particles)
 Additional CL grooves top and second piston ring. Equalizing of
pressure-drop across the ring packages.

MAN Diesel & Turbo PXN LEO  < 14 >


Ultra low sulphur
Operation

Use of Low Sulfur fuel


reduce the corrosive
impact, and give risk of
liner polish

MAN Diesel & Turbo PXN LEO  < 15 >


Ultra low sulphur
Operation

High sulphur fuel (above 4%)


Medium sulphur fuel

Liner wear rate [mm/1000h]


Low sulphur fuel (below 2%)

Oil starvation
Scuffing

Danger area!
0.15

0.07
0.01 Feed rate
Min.feed rate

Max.feedrate
Basic setting

MAN Diesel & Turbo PXN LEO  < 16 >


Cylinder Lubrication
ACOM - Automated Cylinder Oil Mixing

Key points:

HIGH LOW  always optimal dosage


BN BN  always optimal BN (stepless mixing)
 mixing of two approved oils
 correct viscosity
 optimal detergency
 quick change (in/out of SECA)
ACOM
mixing unit

MAN Diesel & Turbo PXN LEO  < 17 >


Cylinder Lubrication
ACOM - automated cylinder oil mixing

Storage tank Storage tank


low BN high BN

ACOM unit

MAN Diesel & Turbo PXN LEO  < 18 >


Cracked EXH valve housing G95ME-
C9.5

MAN Diesel & Turbo PXN LEO  < 19 >


G95 Exhaust Valve Housing
Exh. side – casting directors top

To reduce the stress, flange is changed from 2 bolts, to 4 bolts and round
standard flange.
New round flange have been moved down and towards center

Old New
51.5 mm 5 mm

MAN Diesel & Turbo PXN LEO  < 20 >


Cavitation in Hyd system for EXH valve

MAN Diesel & Turbo PXN LEO  < 21 >


Cavitation near grooves on the EXH
actuator top cover.

MAN Diesel & Turbo PXN LEO  < 22 >


10L TSP Accumulators

 10 failures reported

 Warning letter issued immediately

 Root cause: too sharp thread root

Cross section of the lower shell

Initiation point Crack

MAN Diesel & Turbo PXN LEO  < 23 >


TSP Accumulators

Correction actions

 Design correction by TSP

 FEM validation by MDT

 MDT assistance during testing

 MDT supports QA/QC of production

 All 4856 pcs TSP 10L accumulators


are being exchanged

MAN Diesel & Turbo PXN LEO  < 24 >


Damage to hyd accumulator due to
running with too low pressure

Check pressure and recharge every 2000 hrs.

MAN Diesel & Turbo PXN LEO  < 25 >


New features in ME-ECS

LDCL Integration
 Temporary PComp increase during acceleration.
 Improved start performance
Support for Chinese language
 Integration of Auto Tuning in ECT
 HPS Observer control.
 RPM limiter for cylinder reactivation.
 Screen for Insulation and Noise Pulse Counter.
 Alpha Lubricator MKII
 ME Interface for ME-GI
 Option for SG with Speed Dependent Output Power
 EGR interface
 WHR2
 Support for both fuel leakage and relief disk
 Close position change alarm with Fuel cut out
 Alarm for combined start-up pumps in MASTER-Backup mode.
 Optimised repeated start at crash astern

MAN Diesel & Turbo PXN LEO  < 26 >


CW compared to MBD FIVA Valve.

MAN Diesel & Turbo PXN LEO 2007-01-03


 < 27 >
FIVA Untimed injection due to particle
in FIVA control valve

MAN Diesel & Turbo PXN LEO  < 28 >


Dirt particle caught in FIVA proportional
valve.

MAN Diesel & Turbo PXN LEO  < 29 >


FIVA / ELFI Last chance filter.
In Development, Service test in progress

Purpose:
• To protect FIVA/ELFI pilot valve from
seizure due to foreign particles.
Specification:
• Installed throughout engine life time
• Filter mesh 80 Micron
Status:
• 250 hours test rig completed
• 6 month service completed:
Magleby Maersk, 8S80ME9.2 TII,
Merete Maersk, 7S80ME9.2 TII,
Maersk Mc-Kinney Møller, 8S80ME9.2

Will be introduced spring 2017 pending


positive service test results.

MAN Diesel & Turbo PXN LEO  < 30 >


Service experince FIVA control valve Parker
type 32800 hrs operation. Leak rate 0,46l/min
which is normal and OK

MAN Diesel & Turbo PXN LEO  < 31 >


Evaluation of wear of FIVA proportional
valves during engine running.

MAN Diesel & Turbo PXN LEO  < 32 >


EC MOP – Sticky Touch Issue
Issue:
 Touch pointer sticks

Root cause:
 Failure of glass plate separation

Corrective actions:
 Improved bonding
 Preassembly tests

Verification:
 0.5 % to 1.4 % failure rates after corrective actions

MAN Diesel & Turbo PXN LEO  < 33 >


MPC/MPC10

MAN Diesel & Turbo PXN LEO  < 34 >


 Malfunktion of MPC Channel 70 ,FIVA control ,due to MPC
komponent fail.

MAN Diesel & Turbo PXN LEO  < 35 >


MPC/MPC10
Case story

 Problem:
Increased failure rates from one MPC/MPC10
manufacturer

Data collection:
Investigations and auditing

 Root cause:
Fluxing and soldering processes affected

 Corrective actions:
Temporary production stop. Changes in production
process and QA/QC

 Verification:
> 4000 units produced – return rate ~ 1%

MAN Diesel & Turbo PXN LEO  < 36 >


MPC/MPC10
Emphasis on QA/QC systems implementation

IPC J-STD-001
Production
Requirements

MAN Diesel & Turbo PXN LEO  < 37 >


ME-V
Variable exhaust valve timing for 50 ME-B

Hydraulic push rod…


...extended by adding hydraulic oil

Timing unit

pmax and pcomp

New short cam

20 30 40 50 60 70 80 90 100
Previous cam Load [%]

MAN Diesel & Turbo PXN LEO  < 38 >


ME-V
Deaeration problem during load up

ME-V activated ▼
Pcomp
Incorrect

Correct

Pcomp/Pscav

Pmax

MAN Diesel & Turbo PXN LEO  < 39 >


ME-V
G/S50ME-B9.3 - improved design of ME-V timing piston

Oil supply groove Previous version New version


MAN Diesel & Turbo PXN LEO  < 40 >
ME-V Inductive sensor
ME-B dot 3

• Previous two approved makers of timing unit


sensors – Pepperl & Fuchs / Contrinex
• 661 ME-V engines in service ~ 3900 sensors
• Used for Alpha Lube since year 2000 ~ 100000
sensors
• Pepperl & Fuchs has been preferred by
licensee due to price.

Pepperl & Fuchs Contrinex

Timing unit sensor

MAN Diesel & Turbo PXN LEO  < 41 >


Introduction to the ME-V system
ME-B dot 3

ME-V Versions

Different versions – different problems – different solutions

Mk. 1 Mk. 2 Mk. 3

MAN Diesel & Turbo PXN LEO  < 42 >


High pressure peaks from closing of fuel
injection affecting H.P piping 50ME-B

MAN Diesel & Turbo PXN LEO  < 43 >


Mk.3 HP pipes
ME-B dot 3

 Increased dimension of pipes


 Mounting tools specified

MAN Diesel & Turbo PXN LEO  < 44 >


ELFI Integrator saturation alarms
Parker control valves of analogue type

Problem description:
 ELFI integrator saturation alarm
 No influence on engine running

Root cause:
 Temperature sensitivity of control valve electronics.

 Mechanical wear of pilot piston.

Corrective action:
New engines:
 Valve electronics design changed (digital
electronics)

In service engines:
Replace if mechanical severe worn Recalibration if
thermal drift.

MAN Diesel & Turbo PXN LEO  < 45 >


Inductive sensors
Fuel booster and exhaust valve position

• Claim rates are relatively low


(<1.5%)

• Our work continue to reduce to


target of 0.5 % or better.

• Sensor specification “tightened”


with more strict reliability,
environmental and dynamic
characteristics demands.

• More strict approval procedure.

MAN Diesel & Turbo PXN LEO  < 46 >


Main Bearing damaged due to dirt

MAN Diesel & Turbo PXN LEO  < 47 >


Saved by Main bearing temp alarm

MAN Diesel & Turbo PXN LEO  < 48 >


Main bearing damaged.
Solution Blended edge installed.

MAN Diesel & Turbo PXN LEO  < 49 >


Main Bearings Blended Edge.

The Blended Edge ”BE”, schematically and the specification at drawing.

The width of the ”BE” the distance from C


to B at the drawing, are individual for the
different engine /bearing size.

MAN Diesel & Turbo PXN LEO  < 50 >


Performance of DLF
Dynamic Limiter Funktion.

[Optional] subtitle,
referent and location, date

MAN Diesel & Turbo PXN LEO  < 51 >


Effect of Dynamic Engine Tuning.
Dynamic Limiter Funktion.
Time for Passing barred speed range improved
from 100 s to 20 sec

MAN Diesel & Turbo PXN LEO  < 52 >


Torque Limiter in the Diagram
DLF allows higher temporary load
Standard For ECS cer 1312-5.

MAN Diesel & Turbo PXN LEO  < 53 >


Experince with latest propeller light
running margin on G type engines

MAN Diesel & Turbo PXN LEO  < 54 >


Propeller Trailing edge cutting.

MAN Diesel & Turbo PXN LEO  < 55 >


Tier III Technologies for Two-Stroke Engines
using Oil and Gas

North Sea
English Channel Baltic Sea

Spain
Japan
North America
US Caribbean

Singapore

Adopted NOx ECA


Australia
Future NOx ECA?
NOx reduction with SCR NOx prevention with EGR
SOx Exhaust Gas Scrubber
Selective Catalyst Reduction Exhaust Gas Recirculation April 2014
MAN Diesel & Turbo OG-LS 3339446.2014.05.07
PXN LEO  < 56 >
EGR plant overview

Name Type EGR Fuel EGR Trade pattern


configuratio run hrs.
n
Maersk 6S80ME-C Cut out HFO 3500 Asia↔W. Africa
Cardiff Mk. 9.2 TIII 2 MET T/Cs 1 - 3,5%
Pegasus 6S70ME-C Cut out MDO 80 San Francisco ↔
Voyager Mk. 9.2 TIII 2 MET T/Cs S≤0,1% L.A. ↔ PAL.
Polaris 6S70ME-C Cut out MDO 120 San Francisco ↔
Voyager Mk. 9.2 TIII 2 MET T/Cs S≤0,1% L.A. ↔ PAL.
Key 6S60ME-C By-pass HFO 215 World Wide
Pacifico Mk. 8.2 TIII 1 MET T/C 1 - 3,5%

MAN Diesel & Turbo PXN LEO  < 57 >


EGR on high Sulphur HFO
cylinder condition
 Scrape down indicate some small
CLO penalty, but within control by
lubrication adjustment and air/gas
quality

MAN Diesel & Turbo PXN LEO  < 58 >


EGR on High Sulphur HFO
Dirt Build-up

EGR “Dirt” build up in EGR Suction Chamber, Pipes and EGR Mixing Chamber

The “dirt” is insoluble and has to be scraped out manually.

“Dirt” amount is fuel related: HFO ≈> 1.2 kg/hr Distillates ≈> 0.1 kg/hr (irrespective of
load)

MAN Diesel & Turbo PXN LEO  < 59 >


EGR on Low Sulphur Fuel
Internals after 120 EGR Running Hours

Significant difference from what is


seen when operating on HFO.

MAN Diesel & Turbo PXN LEO  < 60 >


Santa Vista
SCR Service Experience

Issues identified 2011-2013


Boiler clogging when
running on HFO with
 Ammonia slip from SCR reactor gave high NH3 slip
deposits on downstream boiler. Boiler  Rapid buildup of ABS
could not operate with SCR engaged
 Reduce ABS formation by minimizing
ammonia slip

 Corrosion of SCR line during Tier II Boiler issues solved by


operation due to exhaust gas leaks into Reducing ammonia slip
cold SCR system. (improved reactor design)
 Venting of SCR line in Tier II mode
2015
 Tight Valve design Boiler operating well
 Heating during short time • 1000h operation with
disengagement HFO
• 1000h operation with
LSFO

MAN Diesel & Turbo PXN LEO  < 61 >


Yara Kara inside SCR Reactor
Inspection

 Very recently, Yara Kara was


visited for the first time since
delivery from shipyard
 All inspections indicate
healthy condition

MAN Diesel & Turbo PXN LEO  < 62 >


MAN B&W is Leading Tier III Technologist

SCR is proven in service.


Further development with licensees.

EGR is proven in service.


Will be developed to cater for different scenarios:
 EGR for heavy fuel for Tier III compliance and for Tier II
compliance with fuel saving potential
 EGR for max 0.5 % sulphur
 EGR for max 0.1 % sulphur
EGR and SCR is commercially available now.

MAN Diesel & Turbo OG-LS 3339448.2014.05.07


PXN LEO  < 63 >
MAN B&W Low Speed Dual Fuel Engines
Reference List (Ordered)

No. of
Type Mk.
engines
5 S 90 ME-C-GI 10.5
118 G 70 ME-C-GI 9.5 , 9.2
5 L 70 ME-C-GI 8.2
Methane
4 S 70 ME-C-GI 8.2, 7
10 S 50 ME-B-GI / ME-C-GI 9.5, 8.5, 8.2
2 G 45 ME-C-GI 9.5
6 G 50 ME-B-LGI 9.5
Methanol
3 S 50 ME-B-LGI 9.3
5 G 60 ME-C-GIE 9.5
Ethane
3 G 50 ME-C-GIE 9.5
Total dual fuel engines including options: 161 engines

Total power main engine: 2.9 GW

Total dual fuel engines in service: 6 engines


MAN Diesel & Turbo PXN LEO  < 64 >
ME-GI - Service Experience
Operation Hours on Dual Fuel – In Service

Isla Bella
World's First LNG Containership
2 x 8L70ME-GI
Engine builder: Doosan
Yard: General Dynamics NASSCO
Owner: Tote Inc.
Ship type: Container
Capacity/cargo: 3,100 teu
Class: ABS

Milestones

2012, December: Order signed 2015, November: First vessel in service


2014, June: FAT accepted 2016, January: Successful LNG bunkering
2015, July: Mooring trial in diesel mode Running hours HFO/DO: > 4000
2015; August: Sea trial on MDO Hereof running hours LNG: > 1800
2015, October: Official sea trial

MAN Diesel & Turbo PXN LEO  < 65 >


ME-GI - Service Experience
Operation Hours on Dual Fuel – In Service

M/V Creole Spirit


Worlds First ME-GI LNG Carrier
2 x 5G70ME-GI
Engine builder: HHI-EMD
Yard: DSME
Owner: Teekay LNG Partners
Ship type: LNG tanker
Capacity/cargo: 173,400 cbm
Class: ABS

2012, December: Order signedMilestones


2015, January: FAT accepted
2015, October: Sea trial on diesel oil
2016, February: Vessel delivery
2015, December: Official gas sea trial
2016, March: Vessel in service
Running hours HFO: > 2 x 2500
Hereof running hours LNG: > 2 x
2499

MAN Diesel & Turbo PXN LEO  < 66 >


ME-GI - Service Experience
Operation Hours on Dual Fuel – In Service

Rasheeda
World's First Conversion
2 x 7S70ME-C to ME-GI
Engine builder: Doosan Yard
Retrofit yard: NKOM
Owner: Nakilat
Ship type: LNG tanker
Capacity/cargo: 266,000 cbm
Class: ABS

2013, December: Turnkey conversion contract signed


Milestones
2015, April: Ship docking and conversion
2015, May: Sea trial on HFO 2015, September: Vessel in service
2015, September: Initial gas trial performed Running hours since conversion: > 2 x 6000
2015, November: Official sea trial for both engines Hereof running hours LNG: > 2 x 480 ( Dirt in
gas system)

MAN Diesel & Turbo PXN LEO  < 67 >


First succesfully seatrial on Methanol
completed Vestfall – Larsen

The ME-LGI Project


Succesfully Completed
Seatrial with
6G50ME-LGI
Operating on Methanol

Worlds First ME-LGI Methanol


Carrier
M/V LINDANGER Bergen,

MAN Diesel & Turbo PXN LEO  < 68 >


ME-GI-ECS Fuel gas supply system.

MAN Diesel & Turbo PXN LEO  < 69 >


Dual Fuel Injection Control
From Gov Index to injection duration and timing

MAN Diesel & Turbo PXN LEO  < 70 >


ME-GI and ME-LGI Gas Technologies
The ME-GI Engine is a Diesel-Cycle Combustion Engine

Injection and combustion


stability on 4T50ME-X:
 500 consecutive cycles
analysed

 ME-GI marginally better cycle-


to-cycle stability

MAN Diesel & Turbo PXN LEO  < 72 >


8L70ME-C8.2-GI-TII, Service hrs.
3685. Fuel in use Gas or Distillate

Deposit control satisfactory, wear very low


as Alu-coat still present after 3700 hrs

Liner surface
very good

Deposit control by PC-ring is


Sludge residuals in effective as deposits is not
scavenge box is at touching the liner
very low level

MAN Diesel & Turbo PXN LEO  < 73 >


ME-GI - Service Experience
Lubrication System for ME-GI

Automated Cylinder Oil Switch (ACOS)


system

High Low
BN BN

MAN Diesel & Turbo PXN LEO  < 74 >


ME-GI Components

MAN Diesel & Turbo PXN LEO  < 75 >


ME-GI Commissioning Experience
Gas channel sensors

 New type gas channel sensors, atex approved and exchanged on


existing vessels in service.

MAN Diesel & Turbo PXN LEO  < 76 >


Failure of ELGI valve.

MAN Diesel & Turbo PXN LEO  < 77 >


ME-GI and ME-LGI Gas Technologies
ME-GI Development: GIV Hydraulic Leakage - Cause of Failure

MAN Diesel & Turbo PXN LEO  < 78 >


ME-GI and ME-LGI Gas Technologies
ME-GI Development: GIV Hydraulic Leakage - Cause of Failure

MAN Diesel & Turbo PXN LEO  < 79 >


ME-GI and ME-LGI Gas Technologies
ME-GI Development: Design Updates

Service experience
 Gas injection valve - atomiser

MAN Diesel & Turbo PXN LEO  < 80 >


G70MEC-GI Service Experience:
Atomizer layout

G70

MAN Diesel & Turbo PXN LEO  < 81 >


MAN Diesel & Turbo PXN LEO  < 82 >
Leaking non return valve in gas block

MAN Diesel & Turbo PXN LEO  < 83 >


New design Non return line in Gas
block

MAN Diesel & Turbo PXN LEO  < 84 >


Sticking Non return valve in Gas block

MAN Diesel & Turbo PXN LEO  < 85 >


N2 Pressure testing
New design

By drilling a hole into the


middle of the End cover it is
possible to mount a non-
return-valve for example a
minimess.

By drilling holes in the End


cover, it is possible to
connect this new hole to the
gas detection bore.

The classification of the


modification is similar to the
new accumulator in the LPG
engine, which is already
approved by CLASS

MAN Diesel & Turbo PXN LEO  < 86 >


N2 Pressure testing
New design

MAN Diesel & Turbo PXN LEO  < 87 >


Seals for Window valve connector piece
damaged.

 New Betech seal

MAN Diesel & Turbo PXN LEO  < 88 >


Window valve
Hydraulic sealing

Control oil
 0-300 bar, heavy pulsating.
 Peak is measured 600-700 bar
 Oil SAE30
 Temperature 50-80 °C
 Max gap: 0.173mm radial

Sealing oil
 350 bar
 No peak +/- 30 bar
 Oil SAE30
 Temperature 50-80 °C
 Max gap: 0.173mm radial

MAN Diesel & Turbo PXN LEO  < 89 >


GI fuel auxiliary equipment
Auxiliary equipment for GI/LGI

Gas valve train


Gas condition from
FGSS:
Pressure up to 400bar
Supercritical state
”High density and
compressible”

Leak condition:
Gas state with cold
expansion and short
term condensation

MAN Diesel & Turbo PXN LEO  < 90 >


Service experience
The reason for a filter

Due to excessive particles in gas piping after installation:

- dP measurement for HP filter introduced


- Enlarge
Particles andgrinding,
from installation, strengthen
slag etc. existing HP filter Fine particles from LNG, possibly from perlite insulation, and
piston rings on cold ends or GVT seals

MAN Diesel & Turbo PXN LEO  < 91 >


#7 Suction Buffer Vessel and HP pump # 1 strainer inspection
02.01.16

Mixed particles
• Suction Buffer Vessel contaminated with particles of
diverse appearances: wood, plastic, metal, dust, etc.
• Particles were seperated in magnetic and non-magnetic
• The magnetic particles were rinsed and removed from
dust and dirt. These particles are mainly in form of
machining chips, appearing with tempering colors
• Composition of cleaned particles (EDS Analysis):
 Mainly stainless steels (e.g. ASTM 304 and 216) together with
some (Al, Si, Ca,…) oxide compounds and brass alloys Mixed particles Grit blasting particles
 Oxide compounds can be originated from sand/ cement/ perlite
or of similar materials
• Grit grains from the grit blasting were also examined, there were
no other particles mixed with

 For further details see examination report no. N9551A


Magnetic particles Non - magnetic particles

MAN Diesel & Turbo PXN LEO  < 92 >


Actions
Cleaning procedures

Flushing/cleaning procedures

Production specification “Pressure test and cleaning


requirements(0743759-4), applying to supply pipe
systems”, has recently been thoroughly updated by
LEP.

DUN will be issued to stress that it must be possible to


access GVT and engine gas connections for the
purpose of flushing.

For new orders spool pieces will be supplied with the


GVT.

MAN Diesel & Turbo PXN LEO  < 93 >


8L70MEC-GI Service Experience
Gas Valve Train Strainer

The strainer installed in the Gas Valve


Train (GVT) are getting blocked within
short periods of gas operation

Strainer mesh size: 10µm

MAN Diesel & Turbo PXN LEO  < 94 >


Actions
GVT Commisioning filter/Pre-filter

Eltronic has developed a larger GVT filter (20


micron) which can be fitted at the inlet of the
GVT.

This filter can be used during commissioning


or fitted permanently as preferred by the
customer.

MAN Diesel & Turbo PXN LEO  < 95 >


GVT flange connections
Double wall pipe installation

Spool
piece

Fix
support
MAN Diesel & Turbo PXN LEO  < 96 >
Actions
Specifying gas filter

Gas filter in the supply system and bunkering system will be specified.

Requirement: Requirement:
A 10 micron filter is required: Supplier of the FGSS must ensure that
- In the bunker line (“bunkering filter”) OR particles of more than 10 micron have been
- At the suction side of pump (“LP filter”) OR removed from the fuel gas at the outlet of the
- At the outlet side of vaporizer (“HP filter”) FGSS.

LNG Tank FGSS GVT

Recommendation: 20 micron safety filter


Bunkering filter, minimum in line with ‘SIGTTO
Recommendations for the Installation of Cargo
Strainers on LNG Carriers’
ASTM 20 mesh (nominal aperture of 0.84 mm).

MAN Diesel & Turbo PXN LEO  < 97 >


ME-GI and ME-LGI Gas Technologies
ME-LGI Methanol - Development Milestones

TAT at MES 4S50ME-T9


LGI demonstration event
at MDT 4T50ME-X

Test at MES 4S50ME-T9

Sea trial MNS Taranaki Sun


Test at MDT 4T50ME-X Test at HHI 6G50ME-B9.3

Test at MES 7S50ME-B9.3

Sea trial HMD Lindanger

Celebration at MES

Sea trial HMD Mari Jone


Sea trial HMD Leikanger
Sea trial HMD Mari Boyle

2015 2016

MAN Diesel & Turbo PXN LEO  < 98 >


ME-LGI – G50 and S50 methanol engines
Service Experience

Service status: Challenges:


 4 vessels from HHI in service  Broken springs in fuel diesel
 1 out of 3 vessel from MES in fuel valves:
service currently  Broken cut-off shafts I FBIV:
 Currently approx. 400 service  Micro cracks observed in FBIV atomizers:
hours obtained
 Damage of sealing rings in FBIV
 First start up of MeOH operation
was carried out by the crew suction valves:
alone  Unstable HC sensors: Plan B
initiated
 Extensive follow-up will be  Several SW bugs
carried out  have disturbed operation:
 N2 Leaking MeOH accu-
mulators resulting in damage
of membrane

MAN Diesel & Turbo PXN LEO  < 99 >


ME-GI and ME-LGI Gas Technologies
ME-LGI Methanol - Service Experience: 6G50ME-B9.3 LGI

Service experience:
 Shop test on 7 engines
 Currently 300 service hours
obtained
 FBIV works good and
hydraulic components in
good condition
 First start up of MeOH
operation was carried out by Plunger Cut-off shaft
the crew alone
 Extensive follow-up will be
carried out

Atomizer

MAN Diesel & Turbo PXN LEO  < 100 >
ME-GI and ME-LGI Gas Technologies
ME-LGI Methanol - Service Experience: 6G50ME-B9.3 LGI

Challenge: Countermeasure:
Broken springs in diesel fuel injectors due to Under investigation.
high forces during pilot injection when Intermediate solution is to run with
operating on methanol. specified fuel mix using the diesel
injection profile instead of pilot profile.

MAN Diesel & Turbo PXN LEO  < 101 >
ME-GI and ME-LGI Gas Technologies
ME-LGI Methanol - Service Experience: 6G50ME-B9.3 LGI

Challenge: Countermeasure:
Failing HC sensors in cooling sealing oil unit Ensuring that oil level is not exceeding high
caused by contamination of oil due to level alarm level.
overfilling of cooling sealing oil unit.  Visual inspection will be installed in tank
 HC sensors moved to a new location
away from engine.

MAN Diesel & Turbo PXN LEO  < 102 >
ME-GI and ME-LGI Gas Technologies
ME-LGI Methanol - Service Experience: 6G50ME-B9.3 LGI

Challenge: Countermeasure:
SW challenges observed during operation New SW version being corrected and
resulting in false alarms. introduced.

MAN Diesel & Turbo PXN LEO  < 103 >
Vision
Remote services throughout engine lifecycle

Licence builder: Owner:


 online at shop test  condition monitoring
 online at sea trial  performance optimisation
 remote assistance  troubleshooting on demand

Vessel
EMS-
MOP
MDT

LICENSEE
ERCS- ECS-
MOP MOP

OWNER

ENGINE
MAN Diesel & Turbo PXN LEO  < 104 >
EMS – Engine Management Services
The EMS PC – a provision for remote services

EMS
EMS-
+
MOP
PMI Auto-tuning CoCoS-EDS ME Basic

EMS MOP is also:


 enabling remote services

 high security - “hardened platform”

 plug and play interface

 a provision for remote services

MAN Diesel & Turbo PXN LEO  << 105


105 >
>
EMS
Hardened platform

Traditional anti-virus EMS hardened platform


protection

Principle ”Black” listing of ”White” listing of applications


applications and certificates

System Often (“on daily basis”) Not required


updating

System access A new unknown virus is Any program is denied access


allowed access -
Access requires white list and
certificate
System Changes to Windows No persistent change to
modification configuration allowed (also Windows configuration
by unknown virus) allowed (Windows executed
only in memory)
Recover from Update and run anti-virus. Reboot PC
virus Often: Wipe computer, re-
MAN Diesel & Turbo install. PXN LEO  < 106 >
Remote Configuration Update
Automated online ECS parameter update

Challenges:
Need for update of ECS (engine control system) configuration (parameters)

 service experience improvements


 service assistance

Customers expect timely efficient service

Solution: automated online ECS parameter update

MAN Diesel & Turbo PXN LEO  < 107 >
Step 1
Delivery of update by e-mail

E-mail

MAN Diesel & Turbo PXN LEO  < 108 >
Step 1
Delivery of update by e-mail

PUT – Parameter Update Tool:

Used in approximately 30 cases:


100 % positive feedback

Examples of adjustments/ problems solved:


 Cylinder Lubricator settings
 Alarms due to FIVA settings
 Black smoke issue
 Alarms from ME-V system
 Malfunction of CPC system

MAN Diesel & Turbo PXN LEO  < 109 >
Step 2
Delivery by internet directly to vessels EMS

Internet

Preconditions:
 EMS system installed
 Internet connection available

MAN Diesel & Turbo PXN LEO  < 110 >
Step 3
Automated online ECS parameter update

Internet

Preconditions:
 EMS system installed
 Internet connection available
 EC MOP III (being developed)

.
MAN Diesel & Turbo PXN LEO  < 111 >
Cylinder Condition & Performance
On-Board Diagnostic, OBD / CoCoS

OBD combines Systems and


procedures already established ……..
Condition Monitoring.
Wear data of Liners and Relevant engine -and
Piston rings OBD-system alarm data

Engine/vessel
Performance
data
Drain Oil
MAN B&W - Flame Marine Analysis Data

…. and evaluate, and gives


Fuel oil data
expert knowledge and advice in return

MAN Diesel & Turbo PXN LEO  < 112 >
Cylinder Condition & Performance
On-Board Diagnostic, OBD / CoCos

MAN Diesel & Turbo PXN LEO  < 113 >
Cylinder Condition & Performance
On-Board Diagnostic, OBD / CoCos

MAN Diesel & Turbo PXN LEO  < 114 >
Cylinder Condition & Performance
On-Board Diagnostic, OBD / CoCos

MAN Diesel & Turbo PXN LEO  < 115 >
Cylinder Condition & Performance
On-Board Diagnostic, OBD / CoCos

OBD combine and evaluate


on-board data already
present:

• Manual measured wear-


data of piston rings and
ring-grooves
• COCOS data from engine-
and alarm system
• On-board drain oil analyses
or shore based analysis
data
• Guiding overhaul interval

MAN Diesel & Turbo PXN LEO  < 116


116 >
Follow up on engine oil system in
service

MAN Diesel & Turbo PXN LEO  < 117 >
 Improved Hyd Oil cleaning method.
 Replacing the Excisting ME Bypaas filter with FINE filter
inserts

MAN Diesel & Turbo PXN LEO  < 118 >
Sites
Worldwide Locations (Service Centers/Hubs)

>100 global service centers/hubs in >50 countries


MAN Diesel & Turbo PXN LEO  < 119 >

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