Schlumberger provided a morning report from their work on the FARC-11 well. They dismantled the ESP system and found scale buildup and damage. Upon electrical testing, the motor showed an open reading at the pothead indicating burn out. Equipment from the previous FARC-15 well was being backloaded for transport including the ESP system and various tool baskets and casing equipment.
Schlumberger provided a morning report from their work on the FARC-11 well. They dismantled the ESP system and found scale buildup and damage. Upon electrical testing, the motor showed an open reading at the pothead indicating burn out. Equipment from the previous FARC-15 well was being backloaded for transport including the ESP system and various tool baskets and casing equipment.
Schlumberger provided a morning report from their work on the FARC-11 well. They dismantled the ESP system and found scale buildup and damage. Upon electrical testing, the motor showed an open reading at the pothead indicating burn out. Equipment from the previous FARC-15 well was being backloaded for transport including the ESP system and various tool baskets and casing equipment.
Schlumberger provided a morning report from their work on the FARC-11 well. They dismantled the ESP system and found scale buildup and damage. Upon electrical testing, the motor showed an open reading at the pothead indicating burn out. Equipment from the previous FARC-15 well was being backloaded for transport including the ESP system and various tool baskets and casing equipment.
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Schlumberger MORNING REPORT
PT. SCHLUMBERGER GEOPHYSIC NUSANTARA
BARGE : COSL 223
DATE : 12-Jul-20 WELL NAME/ JOB : FARC-11/ WBS NO:OS20D22120 / PUMP REPAIR REASON Field Specialist/ Jusman Indra K R. TIME 105 Days / Hrs Onboard Operator (S) Ahmad K Fendi SHUT IN Days / Hrs RC D1000NX 218STG/VGSA/MAX BPBSL POOH 90 HP - 1516 V -38.7 A + xT 150_1 E.S.P TYPE RC D1000NX 218STG/VGSA/MAX BPBSL RIH /MAX 456, NGM 100/120HP 1069/1283V 62.2A /xT 150_1+Shroud 5.5" @7990FT [PACKER/SSD/RCV]
OPERATION @ 05:00 AM Logging Job by COSL LOGGING
ACTIVITIES ESP Related Activities and Issues RIG/ Barge TIME (05:00 - 18:00) TIME (05:00 - 18:00) 05:00-18:00 Logging Job (Banuwati-02) by COSL Logging
15:30-17:00 Toolbox Inventory and Housekeeping
TIME (18:00 - 05:00) TIME (18:00 - 05:00)
18:00-05:00 Logging Job (Banuwati-02) by COSL Logging
No. Type PN SN Remarks
CABLE ON BOARD
DISMANTLE REPORT VISUAL INSPECTION / ELECTRICAL TEST
PUMP UT Shaft rotation rough, Found Scale on top of pump3, Housing covered by scale PUMP CT Shaft rotation free, Found Scale on top of pump2, Housing covered by scale PUMP LT Shaft rotation free, Found Scale on top of pump1, Housing covered by scale AGH INTAKE/ VGSA Shaft rotation free, No foreign material inside Screen, Housing covered by scale PROTECTOR Shaft rotation free, Empty oil on upper chamber, Dirty Oil at middle and bottom of Protector, Housing covered by scale MOTOR S/R free, Pothead Damaged ,Burn Out from inside,Low Reading (pothead still attached)P-P:OL Ω OL Ω OL ΩP-G: 0.2Ω 0.2Ω 0.2Ω DMT/SENSOR Tool Fault (cLA:0.872,CZ:1.305,CF:1.301), Housing good CASING SHROUD Good Condition, No Corrosive indication, No Broken on Housing or Thread SCREEN
BIW PENT. / CONNECT.
CABLE PACK OFF D.M.T Test on Surface PIP Psig ROUND+ FLAT CABLE Operable Condition, No Broken Armor and Insulation BHT O F Mot T O F ELECTRIC READING BY MEGGER WELL NAME : DATA START P-G PHASE 1 PHASE 2 PHASE 3 DATE / TIME : MOTOR S/A A SBHP PSI D.M.T R/A A SBHT/Tm o F ROUND CBL PUT Minutes FBHP PSI FLAT CBL RTP PSI FBHT/Tm o F ROT. RATE BFPD Pulling Result: Pothead was Damaged, Burn Out, Reading at Pothead OL/Open Last Backload Ex-Well FARC-15 MTD No : T-3301029
Equipment on Board : Equipment for Backload - Jakarta (MTD#)