Nothing Special   »   [go: up one dir, main page]

LNG Badak CO2 Removal Hystory

Download as pdf or txt
Download as pdf or txt
You are on page 1of 28

AGENDA

I. INTRODUCTION
II. STRESS CORROSION CRACKING WHEN USING
MEA
III. SOLVENT CONVERSION FROM MEA TO
FORMULATED UCARSOL CR-402
IV. EROSION CORROSION WITH UCARSOL CR-402
V. EFFORTS TO OVERCOME EROSION
CORROSION WITH UCARSOL CR-402
VI. SOLVENT CONVERSION FROM UCARSOL CR-
402 TO BASF aMDEA
VII. CONCLUSIONS
Introduction (Cont.)

? 1977 FIRST DROP OF LNG FROM TRAINS A AND B


? 1982 CONSTRUCTION OF TRAINS C AND D
? 1987 CONSTRUCTION OF TRAIN E
? 1991 CONSTRUCTION OF TRAIN F
? 1995 CONSTRUCTION OF TRAIN G
? 1997 CONSTRUCTION OF TRAIN H
? 2000 PLANT CAPACITIES :
EIGHT TRAINS (A-H)
LNG = 21.64 MM Tons/Year.
LPG = 1.25 MM Tons/Year (Propane + Butane)
Condensate = 10 MM Barrels/Year.
Introduction (Cont.)

CO2 REMOVAL (AMINE) UNIT

ORIGINAL DESIGN (Trains A & B)


• Feed gas : 305,900 Nm3/h
• CO2 content in feed gas : 5.88% vol.
• Amine solution : MEA, strength max 20% wt.
• Amine circulation rate : 740 m 3/h
• Maximum CO2 slip : 50 ppmv
• Use corrosion inhibitor

AFTER REVAMP (Trains A-D)


• Feed gas: 495,000 nm3/h
• Maximum CO2 content in feed gas : 8% vol.
• Amine circulation rate : 1200 m3/h
• Maximum CO2 slip : 50 ppmv
• Use corrosion inhibitor
Introduction (Cont.)

CO2 REMOVAL (AMINE) UNIT

TO DRIER
OVHD.COOLER

CARBON
OVHD.ACC. TREATER
OVHD.ACC.

OVHD.COOLER SURGE
TANK
MECH.
FILTER 1G-6
WASH
WATER
1G-1

AMINE STRIPPER
CO2
ABSORBER
LP STEAM
TRIM
COOLER
FEED GAS

FINFAN
COOLER

FLASH DRUM
REBOILER
CROSS
BOOSTER EXCHANGER
PUMP
II. STRESS CORROSION CRACKING
WITH MEA

TRAINS A & B
• STARTUP WITH MEA SOLUTION IN 1977
• JANUARY 1986, FIRST CRACK INCIDENT IN AMINE
STRIPPER ON THE LACE WELD WITHOUT STRESS
RELIEF

TRAINS C & D
• STARTUP WITH MEA IN 1983
• MAY 1986, CRACK WAS FOUND IN AMINE STRIPPER IN
TRAIN C NEAR THE MIDDLE CIRCUMFERENTIAL WELD

JANUARY 1986 - MAY 1989


10 UNSCHEDULED SHUTDOWNS BECAUSE OF SCC
III. SOLVENT CONVERSION FROM
MEA TO UCARSOL CR-402

SOLVENT CONVERSION
• TO PREVENT FURTHER LOSSES DUE TO SCC
• CARRIED OUT IN THE PERIOD OF 1990-1991
(TRAINS A-D)
• USED MEA WAS BURNED
• TRAINS E/F STARTED UP WITH UCARSOL CR-402

RESULTS
• NO SCC OCCURRED
• REDUCED STEAM CONSUMPTION
• CO2 SLIP IN TREATED GAS < 5 ppmv
SOLVENT CONVERSION … (Cont.)

Operating Conditions with UCARSOL CR-


402
• AMINE STRENGTH 35% WEIGHT
• AMINE CIRCULATION RATE 1050-1100 m3/h
VELOCITY IN PIPING 5-6 ft/sec (1.5-1.8 m/sec)
• MAXIMUM RICH LOADING 0.35 M/M
• MAXIMUM LEAN LOADING 0.02 M/M
• NO CORROSION INHIBITOR
• ANTIFOAM INJECTION RATE 5-6 LITERS/DAY
(50% Si-BASE AND 50% GLYCOL-BASE)
IV. EROSION CORROSION WITH
UCARSOL CR-402

IN 1995, LOST OF LNG PRODUCTION OPPORTUNITY


EQUIVALENT TO $24MM CAUSED BY:
• REDUCED LNG RATE FOR REPAIR ONE BANK CROSS
EXCHANGERS
• SHUTDOWN AMINE UNIT AND LNG PRODUCTION
USING CROSS LEAN GAS FROM OTHER TRAIN
• EXTENDED DOWNTIME FOR EQUIPMENT REPAIR
Erosion Corrosion ... (Cont.)
Metal Content in Solution
UCARSOL CR-402

140
Train E Train A Train B
120
Train C
Iron Content (ppm)

100 Train F Train D

80

60

40

20

0
0 2 4 6 8 10 12 14 16

Month
Erosion Corrosion … (Cont.)

Equipment Inspection Results

AMINE STRIPPER DAMAGE


• INLET DISTRIBUTOR COLLAPSE
• UPPER TRAY DAMAGE
• VESSEL WALL LEAK

CAUSE
• POOR DESIGN INLET DISTRIBUTOR
• VIBRATION
• CORROSIVE SOLVENT
Erosion Corrosion ... (Cont.)

Equipment Inspection Results

AMINE/AMINE CROSS EXCHANGER DAMAGE


• EROSION CORROSION OF THE CARBON STEEL
CHANNEL BOX, FLOATING HEAD COVER, AND FIXED
TUBESHEETS
• THINNING OF 304 SS TUBES
• SCALE FORMATION INSIDE TUBES

AMINE FLASH DRUM DAMAGE


• EROSION CORROSION ON INTERNAL WALL
• POOR DESIGN OF INLET DISTRIBUTOR
Erosion Corrosion ... (Cont.)

HEAT STABLE AMINE SALTS (HSAS)

• PRIMARILY ACETATE, GLYCOLATE, AND FORMATE


• MAXIMUM ALLOWABLE 0.25% WEIGHT
• NEUTRALIZATION USING CAUSTIC
CAUSE
• OXYGEN INGRESS INTO THE SYSTEM
• RETURNING LEAKING SOLUTION INTO THE SYSTEM
PREVENTION
• NITROGEN BLANKETING
Erosion Corrosion ... (Cont.)

Lean Amine Side Corrosion

LOW-PRESSURE RELATED REGIMES SUCH AS:


• DOWNSTREAM CONTROL VALVE
• INSIDE OF ELBOWS
• INLET TUBES OF FIN FAN HEAT EXCHANGER
V. EFFORTS TO OVERCOME
UCARSOL CR-402 EROSION CORROSION

CHANGING OPERATING CONDITIONS


• INCREASE OPERATING PRESSURE OF AMINE FLASH
DRUM
• REDUCE THE RICH AMINE TEMPERATURE OUTLET
CROSS EXCHANGER

EQUIPMENT MODIFICATIONS
• PARTIAL UPGRADE PIPING MATERIAL FROM CS TO SS
• IMPROVE DESIGN OF INLET DISTRIBUTOR AMINE
FLASH DRUM AND AMINE STRIPPER
• IMPROVE MECHANICAL SUPPORT OF AMINE STRIPPER
INLET DISTRIBUTOR
Amine Flash Drum

Liquid
Wire Screen Level

Splash Baffle

Corrosion
Areas

After Modification
Before Modification with Perforated Pipe
(A) (B)
Efforts … (Cont.)

HIGHER AMINE STRENGTH

INCREASE AMINE CONCENTRATION FROM 35% WT TO


45-50% WT TO REDUCE AMINE CIRCULATION RATE

PROBLEMS
• FOAMING IN CO2 ABSORBER VERY FREQUENTLY
• AMINE STRIPPER LEVEL CYCLING
• EXCESSIVE SCALE FORMATION IN STRIPPER
REBOILER
• EROSION CORROSION WAS STILL OBSERVED DURING
INSPECTION AFTER ONE YEAR
• STRENGTH WAS REDUCED BACK TO 35% WT
VI. SOLVENT CONVERSION FROM
UCARSOL CR-402 TO BASF aMDEA

SELECTION OF ALTERNATE SOLVENT


• Corrosion problem is the driving force for solvent
conversion
• Several alternate solvents were evaluated
• Comparison study with reference plants using the
alternate solvent in the U.S. And Europe

SELECTED BASF aMDEA


• Minimum equipment modification is a must
• Test in one train for 18 months, with internal inspection
after 12 months
• Tighter guarantee figures:
- 20 mpy max corrosion rate by coupon
- 100 ppmw max iron content in solution
- No defect found after one year test
Solvent Conversion … (Cont.)

TEST PREPARATION FOR THE


SELECTED SOLVENT

• MAJOR EQUIPMENT INSPECTION FOR BASE LINE


• INSTALL TWO NEW BUNDLES OF CROSS EXCHANGER
TO MEASURE TUBE THINNING RATE & SCALE
FORMATION
• INSTALL THREADED CONNECTIONS ON PIPING FOR
COMPARISON WITH UCARSOL CR-402
• CHEMICAL CLEANING WITH CAUSTIC 2% WT (pH 12)
• STEAM CONDENSATE FLUSHING FINISH
Solvent Conversion … (Cont.)

NEW OPERATING CONDITIONS

• SOLUTION STRENGTH 40% WT


• AMINE CIRCULATION RATE : 750 m3/h, LIMITED BY
CO2 SLIPPAGE INSTEAD OF RICH LOADING
• NO CORROSION INHIBITOR
• MAXIMUM RICH AMINE LOADING : 0.62 M/M
• MAXIMUM LEAN AMINE LOADING : 0.03 M/M
• ANTIFOAM INJECTION RATE 5 LITER/DAY
(GLYCOL TO SILICON BASE 50:50)
Solvent Conversion … (Cont.)

AMINE CIRCULATION RATE

• DESIGN AMINE CIRCULATION: 1200 m3/h


• THREE CIRCULATING PUMPS, TWO RUN
• PUMP CAPACITY: 400-800 M3/H EACH
• REQUIRED CIRCULATION RATE BY PROCESS: 750 M3/H
• PUMP LIMITATION
RUNNING 1 PUMP: LOW PLANT RELIABILITY
RUNNING 2 PUMPS: CLOSE TO MINIMUM FLOW
• TEMPORARY SOLUTION: INCREASE AMINE
CIRCULATION RATE TO 850-900 m3/h
Solvent Conversion … (Cont.)

IRON CONTENT IN aMDEA BASFSOLUTION

4
Fe content (ppmw)

0
Solvent Conversion … (Cont.)

ONE YEAR WARRANTY SHUTDOWN

• NEGLIGIBLE CORROSION ATTACK


• GOOD CONDITION OF THREE THREADED CONNECTIONS
• NO THINNING TUBES IN CROSS EXCHANGER
• NO SCALE FORMATION INSIDE CROSS EXCHANGER
TUBES
Solvent Conversion … (Cont.)

ADVANTAGES OF OPERATING WITH


BASF aMDEA

• AMINE CIRCULATION RATE


28% LOWER THAN UCARSOL CR-402
25% LOWER THAN MEA
• CORROSION RATE
3 MPY MAX CORROSION RATE BY COUPON
MEASURED EVERY 4 WEEKS FOR 6 TIMES
• SOLVENT LOSSES
46% LOWER THAN UCARSOL CR-402
67% LOWER THAN MEA
Solvent Conversion … (Cont.)

ADVANTAGES ...

160

UCARSOL
Iron Content (ppmw)

120

80

40

aMDEA BASF
0
Solvent Conversion … (Cont.)

ADVANTAGES...

COMPARISON OF OPERATING CONDITIONS IN MEA,


Ucarsol AND aMDEA BASF
OPERATING CONDITIONS MEA Ucarsol aMDEA BASF
LNG Rate, m 3 /h 620 725 725
CO2 Slipage, ppmv 15 <10 <10
Amine Circulation Rate, m 3 /h 1000 1050 750
Concentration, %(wt) 20 35 40
Lean Loading, m/m 0.12 0.019 0.012
Rich Loading, m/m 0.41 0.34 0.42
Steam Consumption, Tons/h 125 120 96
Amine Make up, drums/month 23 14 7.5
CONCLUSIONS

• MEA in 1977-1989: SCC occurred in CO2 Absorber and


Amine Stripper and caused 10 unscheduled shutdowns
in January 1986 - May 1989
• UCARSOL CR-402 eliminated SCC but Erosion Corrosion
was prominent. The suspected cause:
CO2 liberation on rich amine side
Vena contracta effect on lean amine side
High linear velocity
• Efforts to control erosion corrosion UCARSOL CR-402 :
Changing operating conditions
Modifying equipment
Upgrading materials
CONCLUSIONS

• Solvent conversion from UCARSOL CR-402 to BASF


aMDEA was successful.
Meet the specified absorption capability
Low corrosion rate by coupon
Lower iron content in solution
Lower steam consumption
Lower solvent makeup
• Lower amine circulation rate could not be maintained
because of pump limitation. Evaluation is being
continued.

You might also like